You are not logged in or registered. Please login or register to use the full functionality of this board...


C.E. Niehoff & Co. Regulator
#21

Had intermittent generator shut down issues on our Kohler that ended being an in-line diode for the fuel solenoid wire.
Reply
#22

All is good. 13.2 V +/- all day long.
500 miles or so with rebuilt alternator and new regulator and we are happy.
Have not had to run Generator at same time, so I don't know if the problem was related and fixed or separate. 500 miles more by the end of the week and I will report back if the generator continues with a problem.

Dave, Karen, w/Buddy and Moose. 
06' Newell #784
towing a 06' Featherlite enclosed trailer or
05' Featherlite stacker for toys and tools, 
or a 21' F350 Big Grin w KTM 300, & MTB
35' Packard 4 dr convertible
59' Nash Metropolitan
I like engines and wheels

Carpe Diem. Have Fun
Tomorrow is not guaranteed.
Reply
#23

Good to hear the results. Thanks for reporting back.

Richard and Rhonda Entrekin
99 Newell, 512
Maverick Hybrid Toad
Inverness, FL (when we're home Cool )
Reply


Forum Jump:


Users browsing this thread: 1 Guest(s)